danturbo4311
Member +
Hello everyone, Im having a problem with fuel getting into the oil on my freshly rebuilt forged 4e which has done just over 400 miles (still running it in) has anyone else had a problem like this when running there engine in as im not sure if its because the rings have not bed in properly yet or because there is a problem. Its not a lot of oil but enough to smell it in the oil & the level is slowly going up.
During the rebuild I had the following parts fitted
Billet cams, uprated valve springs with titanium retainers.
spring base pressure adjusted to within tolerance & head reshimmed.
Head ported & polished & lots of chamber work
ARP headbolts, 1.9mm Athena headgasket, scat conrods, wiscoe 74.5mm pistons, All new bearings, piston rings (all gapped to the spec sheet) block honed.
Im still running it on 10w40 mineral oil & Im also using my 460cc injectors however I have a wideband & I have got it idling at 14.7 to late 15s when hot & 14.1ish when cold. The injectors were leak & flow tested when the rebuild took place & all were fine.
I have already done a compression test & the results were
1 10bar
2 9.5 bar
3 10bar
4 10bar
The compression results dont seem to sad maybe a little low due to the chamber work, 1.9m headgasket & low comp pistons, any input is welcome
During the rebuild I had the following parts fitted
Billet cams, uprated valve springs with titanium retainers.
spring base pressure adjusted to within tolerance & head reshimmed.
Head ported & polished & lots of chamber work
ARP headbolts, 1.9mm Athena headgasket, scat conrods, wiscoe 74.5mm pistons, All new bearings, piston rings (all gapped to the spec sheet) block honed.
Im still running it on 10w40 mineral oil & Im also using my 460cc injectors however I have a wideband & I have got it idling at 14.7 to late 15s when hot & 14.1ish when cold. The injectors were leak & flow tested when the rebuild took place & all were fine.
I have already done a compression test & the results were
1 10bar
2 9.5 bar
3 10bar
4 10bar
The compression results dont seem to sad maybe a little low due to the chamber work, 1.9m headgasket & low comp pistons, any input is welcome
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